Having already laid them in to find the right wire for each pot I set about fitting the ends.
The sequence is this:
1. Cut to length.
2. Use strip tool supplied to strip insulation away.Clever tool this, you just twist it until 9mm of wire pokes out the end, then grip the wire to stop it going through to toll and twist a couple more turns. Pull and off come the insulation.

3. Fold over core and crimp on terminal. (Fold down terminal ears with long nose pliers)
4. Apply silicone lube and slip on boot.
5. Fit to distributor cap.
6. Repeat for all remaining leads.
7. Apply air cleaner with Ford wing nut and stand back to admire tidy wire layout on nearly finished engine.

This however is where it went a bit wrong.
Whilst fixing the wires I followed good old Tom's book, what I didn't check was what I was doing!
I followed the instructions for the HEI ignition module used by Ford, this does not connect the wires in the firing order as the dizzy rotor turns, therefore my firing order is now wrong!
Thinking about it logically I would have realised that something was not right but I was too eager to get it finished, in future I need to think a bit more first!
Luckily for me Ive only had to move four wires around but it has mucked up my tidy layout, still cant be helped. (picture to follow).













Fuel system including fittings and pipe also to be used for PCV.
First problem encountered as I purchased the hose finishes for -6 pipe not realising that this -6 pipe has a larger OD, therefore I need the finishers for the -8 pipe! Another order beckons!






All that remains to do is paint it red to match the block and hide the marks on it where it slipped in the vice.
Here's No.5 inlet is being adjusted (I think it's the inlet!). Basically you tighten the nut down until the push rod just stops turning, then tighten 3/4 of a turn more and lock down the allen grub screw. The 3/4 of a turn puts the correct pre-load on the lifter.

Correct camber is 0 - 1° negative, so Im going to leave at this for now.
Here I figure I have about 4.5° caster, GD manual say about 4° so I will see how I go with 4.5°.
Measure the distance at front of the angle and then at the rear, rear minus front equals toe in. 
So all I did was wind the two tie rods until my laser lined up on the T2 points.
Here we are at "ride height" the floor bar corrected to be level with the disc bar.
Measuring the actual range that this effect started to take place shows it to be over the last 1/2 to 1" of travel. I attempted to resolve the bump steer by moving the rack but I could not eliminate it as my rack was already at its maximum adjustment position. If this becomes a problem on the road Ill reset the steering with the rack in the mid position to give some adjustment.
(Blogspot posting system is really screwed today, each picture I insert adds about 5 carriage returns to each line of the post!)
For the rear most mount I have left the bolt 