Tim very kindly offered to put the motor back on the dyno to run out the water from the engine. So this time father in law accompanied me on the trip to Market Drayton.
All went well this time, fired up straight away again and started to steam as it ran, but this time no more water entered the oil and it gradually cleaned out. Each check of the stick showed less water and clean oil, great news.
Also picked up a few more horses and torques on the way making 336bhp and 330 ft/lbs. Wahey!
However as always the good bad balance was restored when an oil leak started at the rear main seal area.
With the engine off it looked initially like the flywheel bolts might be to blame but after getting the motor home and filling it with oil to store it the leak was clearly evident. So this is why the next post will be called Leak repair 2. See I told I knew why the first one was called 1!!
Any how I did get some video of the engine on a run with me in the dyno cell, its in this short video I put together to show the family what I've been up to.
Enjoy..
Saturday, 31 May 2008
Leak Repair 1.
It says Leak Repair 1 because I'm writing this retrospectively and know what's coming next!
Well I put the engine stand back up and set about finding out where the water leak came from, first off it was evident that the final run really mixed things up.
Obvious candidate was the intake to head seals so off came the top end. All looked OK with no obvious path for water to have made it to my oil. Looking on www.Ford uscle.com I found others talking of oil leaks caused by poor head gaskets, and in particular the Mr Gasket's that I had used. The oil leak in question matched the slight leak which had developed on both heads during the dyno runs. So I travelled further down and removed the first head. What I found was not pretty, the entire deck surface was wet and there was obvious signs of combustion gasses leaking over the cylinder seals.
It looks like the water had found its way under the gaskets and into the oil drain back holes, a slow leak at first which just got worse.
So I purchased some nice new Fel Pro gaskets which just looked better, clear sealing material on both sides in all the right places.
With those in place I set about cleaning the heads and intake of old silicone, what a job! Any way eventually it was all clean and I could re-assemble.
As well as the water leak my sump was leaking oil as well so that came off and what do you know, Mr Gasket had let me down again. This time the Ultraseal one piece gaskets just didn't do the job.
So again new Fel Pro gaskets were used (thanks Tim) with plenty of sealant.
So it was all fixed and ready to be tested again.
Well I put the engine stand back up and set about finding out where the water leak came from, first off it was evident that the final run really mixed things up.
Obvious candidate was the intake to head seals so off came the top end. All looked OK with no obvious path for water to have made it to my oil. Looking on www.Ford uscle.com I found others talking of oil leaks caused by poor head gaskets, and in particular the Mr Gasket's that I had used. The oil leak in question matched the slight leak which had developed on both heads during the dyno runs. So I travelled further down and removed the first head. What I found was not pretty, the entire deck surface was wet and there was obvious signs of combustion gasses leaking over the cylinder seals.
It looks like the water had found its way under the gaskets and into the oil drain back holes, a slow leak at first which just got worse.
So I purchased some nice new Fel Pro gaskets which just looked better, clear sealing material on both sides in all the right places.
With those in place I set about cleaning the heads and intake of old silicone, what a job! Any way eventually it was all clean and I could re-assemble.
As well as the water leak my sump was leaking oil as well so that came off and what do you know, Mr Gasket had let me down again. This time the Ultraseal one piece gaskets just didn't do the job.
So again new Fel Pro gaskets were used (thanks Tim) with plenty of sealant.
So it was all fixed and ready to be tested again.
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